following error question


Hi again,
 
In anticipation of getting the pulse multiplier for my Gecko drive, I installed BDI-EMC on a 1.4 ghz athlon thunderbird machine.  I then setup the emc.ini file with steppermod.o and input scale and output scale set to 5000.  I set the max velocity to 10, and ran EMC.  Much better performance as far as the slugishness of the interface.  When I tried to manually jog the motor 1 inch, I got a following error after it had moved part way.  Are there any other variables using steppermod that I should try?
 
Richard
 


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